Technical Library

Document Type

Water Depth

12/16/2007

Implement an ESeal solution that would enable targeted completion with packer seats while also repairing the damaged vertical section of casing in the Barnett.

06/08/2011

This casing failure occurred during the 13th stage of the well’s plug-&- perf frac job of it’s 4,500 ft lateral section.  To avoid killing the well with potentially damaging weighted fluids, a rig assist snubbing unit was used to enable live-well operations including milling out the casing...

11/21/2013

An Operator, in the Permian, discovered they did not obtain cement coverage along the entire length of the lateral after cementing their production casing.