Technical Library

Objective

09/14/2002

Install larger, corrosion-resistant production conduit.

04/21/2004

Regain pressure integrity of the 7-3/4 in. production liner for stacked FracPac™ completion operations using Solid Expandable Tubular (SET™) technology.

05/05/2006

Get back on planned drilling program and finish the well with an adequate hole size to evaluate potential production zones at TD.

09/12/2004

Solid expandable tubular technology presents an opportunity to significantly boost the production capacity of wells by increasing the size of the completion. As such, it offers an economically attractive and environmentally friendly option to breathe new life into gas fields. It is flexible in...

12/29/2009

A major operator was sidetracking out of an existing well to a nearby reservoir.The first attempt to sidetrack utilizing a conventional casing design failed to reach the target depth and damaged the 13-3/8 in. casing.

The casing design for a...

09/01/2013
In the Marcellus Shale, fracturing rates and pressures can be substantial, but there are other problems also associated with completing these wells, which can promote casing failure or compromise the pressureintegrity of a well. A...
11/04/2011

The ESeal Liner provided the maximum flow area for injector fluids resulting in greater injection volumes and rates due to less friction pressure loss during injection.  The standard conventional scab liner is the 5 in. liner which provides a 4.481 in. ID., while the 5½ x 7 in. ESeal liner...

04/11/2007

A Corrosion across the entire 1,100 ft. of 7 in. casing installed in a natural gas liquids (NGL) storage cavern risked NGL leakage into the surrounding formation.

12/01/2009

In the first stage of the fracturing program, the uppermost fracture sleeve failed - leaving the economic viability of the wells at risk.

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